炼油技术与工程 ›› 2021, Vol. 51 ›› Issue (1): 33-36.

• 机械设备 • 上一篇    下一篇

Shell重油气化装置运行总结

陈平平   

  1. 福建联合石油化工有限公司,福建省泉州市 362800
  • 收稿日期:2020-05-15 修回日期:2020-10-26 出版日期:2021-01-15 发布日期:2021-07-16
  • 作者简介:陈平平,中级工程师,本科,2006年毕业于厦门大学化学工程与工艺专业,现从事部分氧化法制氢装置生产运行管理工作。E-mail:chenpingping@fjrep.com。

Operation summary of Shell heavy oil gasification unit

Chen Pingping   

  1. Fujian Refining and Petrochemical Co., Ltd., Quanzhou, Fujian 362800
  • Received:2020-05-15 Revised:2020-10-26 Online:2021-01-15 Published:2021-07-16

摘要: 某公司重油气化装置采用壳牌(Shell)新重油气化工艺,以脱油沥青为进料,设计硫质量分数6.8%,灰分0.18%,250 ℃ 动力黏度 300.0 mPa·s,是Shell在运重油气化装置中进料性质最差、单炉负荷最高、总规模最大的装置。该装置高度自动化可实现“六年一修”,其关键设备——气化主烧嘴寿命最长可达8 736 h。对装置投产以来遇到的重大问题及相应解决措施进行了介绍,并对装置运行情况进行了评价。基于该气化装置已实现的长周期运行业绩,提出采用重油气化工艺解决目前炼油厂面临的减压渣油、催化裂化油浆、乙烯焦油、渣油加氢未转化油的出路问题。

关键词: Shell, 重油气化装置, 新SGP工艺, 三级状态转移图

Abstract: The heavy oil gasification unit of a company adopts Shell new heavy oil gasification process with deoiled asphalt as feedstock. The designed sulfur content is 6.8%, ash content is 0.18% and dynamic viscosity at 250 ℃ is 300 mPa·s. It is the shell heavy oil gasification unit with the worst feedstock quality, the highest single gasifier capacity and the highest total scale plant. The device is highly automatic and can realize once repair every six years. The life time of gasification main burner which is the key equipment can achieve 8 736 hours. The major problems encountered since the unit is put into operation and the corresponding solutions are introduced, and the operation of the unit is evaluated. Based on the long-term operation performance of the gasification unit, the heavy oil gasification is recommended to solve the outlet issue of vacuum residue, catalytic cracking slurry, ethylene cracking tar, residue hydrotreated unconverted oil from the refinery.

Key words: Shell, heavy oil gasification unit, new SGP process, three-stage state transition diagram