炼油技术与工程 ›› 2024, Vol. 54 ›› Issue (6): 38-42.

• 机械设备 • 上一篇    下一篇

乙烯装置裂解气压缩机段间冷却器腐蚀原因分析

马红杰, 周尖, 丁少辉, 陈永伟, 赵磊   

  1. 1.中国石油独山子石化分公司研究院; 2.中国石油独山子石化分公司乙烯一部
  • 收稿日期:2024-01-29 出版日期:2024-06-16 发布日期:2024-06-27
  • 作者简介:马红杰,高级工程师,硕士,2005年毕业于中国石油大学材料科学与工程专业,现从事腐蚀监检测与防护工作。联系电话:18116970750,E-mail:yjy_mhj@163.com。

Analysis of corrosion reasons for interstage coolers of cracking gas compressors in ethylene plant

Ma Hongjie, Zhou Jian, Ding Shaohui, Chen Yongwei, Zhao Lei   

  1. 1.Research Institute of PetroChina Dushanzi Petrochemical Co., Ltd.; 2.Ethylene1 of PetroChina Dushanzi Petrochemical Co.,Ltd.
  • Received:2024-01-29 Online:2024-06-16 Published:2024-06-27

摘要:

乙烯装置压缩单元三段、四段段间冷却器E-3113、E-3114管束外壁腐蚀严重,影响了装置的长周期、安全运行。采用宏观腐蚀检查、化学成分分析、金相组织分析、腐蚀产物分析等方法对段间冷却器管束进行了腐蚀监检测分析,结果表明:管束进口部位结焦较多,局部管束表面腐蚀坑连接成片,导致管束表面腐蚀减薄严重,段间冷却器管束的腐蚀形式主要是酸腐蚀以湿硫化氢为主,腐蚀介质分压、管束表面结焦及相变区露点腐蚀共同促进了管束的腐蚀。采取了在一至四段段间冷却器壳程入口前加注中和型缓蚀剂的工艺防腐蚀措施,结果表明:段间冷却系统凝液平均pH值由采取措施前的5.23上升至采取措施后的7.91,并稳定控制在7.0~9.0,铁离子质量浓度小于1.0 mg/L,系统酸性腐蚀介质被中和,腐蚀减缓。此外,管束电涡流抽检结果表明,92%的换热管壁厚无明显减薄,且管束自2019年投用至今未发生腐蚀泄漏,系统工艺防腐蚀效果较好。

关键词: 乙烯装置, 裂解气, 压缩机, 段间冷却器, 腐蚀, 硫化氢, 结焦, 相变

Abstract:

The outer walls of the E-3113 and E-3114 intercoolers in the compression unit of the ethylene plant had suffered severe corrosion, affecting the long-term and safe operation of the unit. Macroscopic corrosion inspection, chemical composition analysis, metallographic structure analysis, and corrosion product analysis were used to conduct corrosion monitoring and analysis on the interstage cooler tube bundle. The results showed that there was more coking at the inlet of the tube bundle, and local corrosion pits on the surface of the tube bundle were connected in sheets, resulting in corrosive thickness reductionof the tube bundle. The main reason for the corrosion of the interstage coolers tube bundle was acid corrosion, mainly caused by wet hydrogen sulfide. The partial pressure of the corrosive medium, surface coking of the tube bundle, and dew point corrosion in the phase change zone jointly promoted the corrosion of the tube bundle. A process anti-corrosion measure was taken by adding a neutralizing corrosion inhibitor before the inlet of the shell side of the first to fourth interstage coolers. The results showed that the average pH value of the condensate in the intercooler system increased from 5.23 before the measure was taken to 7.91 after the measure was taken, and remained stable at 7.0~9.0. The concentration of iron ions was less than 1.0 mg/L, and the acidic corrosive medium in the system was neutralized, slowing down corrosion. In addition, the eddy current inspection results of the tube bundle showed that 92% of the heat exchange tubes had no significant wall thickness reduction, and there has been no corrosion leakage of the tube bundle since it was put into use in 2019, indicating a good anti-corrosion effect of the system process.

Key words: ethylene plant, cracking gas, compressor, interstage cooler, corrosion, hydrogen sulfide, coking, phase transition