Petroleum Refinery Engineering ›› 2024, Vol. 54 ›› Issue (10): 22-25.
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Qi Hengshan, Li Desheng, Xie Zheng, Li Linsheng, Liu Zhaoyong
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齐恒山,李德生,谢铮,李林生,柳召永
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Abstract: A 2.8 MMTPY heavy oil catalytic cracking unit in a refinery has been undergoing slurry recycling for about six months under low processing capacity. The recycling method involves injecting the recycled slurry into the mixed feed oil at the feed self-protection assembly, and then into the feed oil nozzle. After calibration, the yield of coke increased from 7.86% to 8.41%, accounting for about 20% of the recycled slurry to produce coke. The diesel yield of the unit increased, and about 50% of the recycled slurry was converted into high-value diesel products. The overall conversion rate of the unit decreased due to slurry recycling, with a total reduction of 1.93 percentage points in the yields of dry gas, liquefied petroleum gas, and gasoline. During the slurry recycling process, the feed oil and reaction system were monitored, and no significant impact was found on the reaction system coking, flue gas turbine operation, feed oil pipeline, and nozzle wear. Subsequent defect elimination inspections also found no abnormalities. Overall, the recycling of slurry in the heavy oil catalytic cracking unit can increase the unit's coke yield, ensure steam balance in the entire plant under low processing capacity, and significantly reduce the solid content of slurry, which helps to reduce the unit's slurry yield.
Key words: font-family:-apple-system, blinkmacsystemfont, ", font-size:14px, background-color:#FFFFFF, ">heavy oil catalytic unit, low processing capacity, slurry recycling, coke, diesel, solid content of slurry, concentration of dust in flue gas
摘要: 某炼油厂2.80Mt/a重油催化裂化装置在低负荷情况下进行了为期约6个月的油浆回炼,回炼方式是将循环油浆在原料自保组立处打入混合原料油中,再进入原料油喷嘴。标定结果表明:焦炭收率由7.86%升至8.41%,占比约20%的回炼油浆生成了焦炭;装置柴油收率提高,占比约50%的回炼油浆转化成高附加值产品柴油;油浆回炼导致装置总转化率下降,干气、液化石油气、汽油收率共降低1.93个百分点。油浆回炼过程中,对原料油及反应系统进行了监控,未发现其对反应系统结焦、烟气轮机运行、原料油管线及原料喷嘴磨损等有明显影响,后续消缺过程中对反应-再生系统内部检查也未发现异常。总体来看,该重油催化裂化装置进行油浆回炼可以提高装置焦炭收率,保证低负荷下全厂蒸汽平衡,可显著降低油浆固含量,有助于降低装置油浆收率。
关键词: font-family:-apple-system, blinkmacsystemfont, ", font-size:14px, background-color:#FFFFFF, ">重油催化裂化装置, 低负荷, 油浆回炼, 焦炭, 柴油, 油浆固含量, 烟气粉尘浓度
Qi Hengshan, Li Desheng, Xie Zheng, Li Linsheng, Liu Zhaoyong. Analysis on the influence of slurry recycling with low processing capacity in a heavy oil catalytic cracking unit[J]. Petroleum Refinery Engineering, 2024, 54(10): 22-25.
齐恒山, 李德生, 谢铮, 李林生, 柳召永. 某重油催化裂化装置低负荷工况油浆回炼影响分析[J]. 炼油技术与工程, 2024, 54(10): 22-25.
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